Tried holding power on already to check for hot or even warm motor/ wires. The old plug had black, blue, and yellow (pretty sure).
Regardless, I wired new plug black 2-black, red 2-red. Matches all around- wires from battery compartment, new plug set, and wires from TM pedal.
I again went underside of the pedal, and this time was able to confirm the same 25.3V at various points. I noticed that the clips on at least 5 connections could be "wiggled". That didnt seem right to me, and I was hopeful I was onto something. I removed, then re-attached perhaps 7 all told, after crimping them for a tight fit. Alas, no change. It is so emphasized to use certain gauge wiring for these rigs, and for ex., even 6 g. min.(?) for the 12V- to 12V+ between 2 batteries. I used 4 gauge. Battery to bow is 8 gauge. But then to look into the pedal- you see these very small wires running to the TM, and find loose fitting clips!! Go figure!??
I moved to the batteries, as I was bad.... letting them site for a few months. I KNOW!!?? But they sit around in the stores, dont they?? (ok, there's the temp control inside the store. Is that It!?) Anyway, having been off the onbaord charger for about 6 days, I tested the fluids using a hydrometer. About half (6) were right on 1.225, while the other 6 varied from 1.218 (guesstimate), to 1.235. Not a concern with the range differences, but other than that, not sure what I can make of it all. On the tester, these values were in the FAIR range, I guess because the 2 batteries measured 12.66V, and 12.68V. I believe that's in the 75% charged range. Surely they'd still be pushing the TM under actual usage, if a bit slower. I'm sure these factors were a bit higher a couple days ago when I first tried, and failed to see the thing operate.
I almost removed the head of the TM, to see if anything obvious leaped out at me.(besides the spiders and frogs here, that seem to be everywhere!!) A fuse? Disconnected / loose clip? I'm about to head out and take the motor to a repair guy to check it out. Should I have at least separated the 2 shaft parts, and tried to test for voltage on any down-bound wiring?